I have a couple of displays planned so I thought, based on this previous experience, I should test run the 3cc vertical single. It started off ok and would drive my light bank (12W) fairly steadily. The performance then dropped off quite rapidly until it would no longer power the lights

After a bit of checking I found a total loss of compression and a hiss from the exhaust when the engine was turned. As it is normally electrically started via the generator I don’t get to feel the compression, but I did turn it by hand to check the valve clearances before starting this test. They were around 0.08 mm, a little tight maybe but should be ok on this engine. I would normally set 0.1mm.
I drained the cooling water and took the head off. The cylinder bore looked ok (for this engine) and blocking the top of the bore gave good compression. Blowing down the exhaust pipe produced bubbles around the valve.
https://youtube.com/shorts/PY2_B0iIkjc?feature=shareI then removed the exhaust valve, the seating and the valve face had an odd mottled appearance. The seating cleaned up well with the original seat cutting tool, made from an M4 caphead screw in the same way as the valves.
The valve was polished with a fine diamond file but this didn’t remove the mottled finish so I recut the seat in the lathe. I also improved the under head profile of the valve.
Next step lap the valves into the seats, clean it all up, and reassemble.